首页> 外文期刊>Tunnelling and underground space technology >Soil-water inrush induced shield tunnel lining damage and its stabilization: A case study
【24h】

Soil-water inrush induced shield tunnel lining damage and its stabilization: A case study

机译:涌水诱发盾构隧道衬砌破坏及其稳定:案例研究

获取原文
获取原文并翻译 | 示例
           

摘要

This paper reports a case study on shield tunnel lining damage induced by soil-water inrush occurred in Tianjin Metro Line 1, China through both field monitoring and numerical simulation. This incident was triggered by the non-watertight boring work of thru holes adjacent to the cross passage between the twin tunnels. Under high hydraulic gradient, the seepage-prone weak zone was formed and extended, then the outburst of soil-water slurry was occurred. Measures including plugging engineering cotton, injecting quick-setting cement and welding partition plate of steel segments, had been taken but in vain. The outburst of soil-water slurry induced soil movement around the cross passage, thus leading to the damage of tunnel lining and ground surface settlement. After sealing the water ingress holes, stabilization methods including surface grouting and inside tunnel back grouting were applied. The mechanisms of segment lining damage and the effectiveness of stabilization are investigated through both numerical simulation and field monitoring data analysis. Lessons learned from this incident have been discussed, thus providing reference for potential shield tunnelling under similar engineering conditions.
机译:本文通过现场监测和数值模拟,对中国天津地铁1号线发生的因水涌引起的盾构隧道衬砌破坏进行了案例研究。该事件是由双隧道之间的交叉通道附近的通孔的非水密钻孔作业触发的。在高水力梯度作用下,形成并扩展了易于渗漏的薄弱区域,然后发生了水土浆的突伸出来。已经采取了一些措施,包括封堵工程棉,注入速凝水泥和焊接钢段隔板,但徒劳无功。水土浆的爆发引起土壤在交叉通道周围的运动,从而导致隧道衬砌和地表沉降的破坏。密封进水孔后,采用包括地面灌浆和隧道内反灌在内的稳定方法。通过数值模拟和现场监测数据分析,研究了分段衬砌破坏的机理和稳定效果。已经讨论了从该事件中汲取的教训,从而为在类似工程条件下进行潜在的盾构掘进提供了参考。

著录项

相似文献

  • 外文文献
  • 中文文献
  • 专利
获取原文

客服邮箱:kefu@zhangqiaokeyan.com

京公网安备:11010802029741号 ICP备案号:京ICP备15016152号-6 六维联合信息科技 (北京) 有限公司©版权所有
  • 客服微信

  • 服务号