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The comparison of performance of bidboland gas refinery unit based on the current designing and the new designing

机译:基于当前设计和新设计的投标天然气精炼装置的性能比较。

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One of the problems of Bidboland Gas Refinery especially in the cold seasons is the low temperature of the sour gas entering to Gas Refinement Unit that .This problem has a direct influence on output reduction of Amin-Amin Exchanger leading to an increase in gas fuel consumption in the Reboiler of Amin Recovery Tower because Amin-Amin exchanger is not able ,in the current condition ,to warm up Rich DEA solution to optimum temperature based on design of the manufacturer company .In order to solve this problem, the Amin-Amin exchanger was redesign by use of Aspen Hysys specialized software and it was used in the process by use of the Aspen Hysys software .Based on the obtained results, in case of using the new exchanger ,the Rich DEA solution temperature will increase from 33°C to 98°C that this increase in temperature causes a 33.2% reduction in gas consumption in the Reboiler. On the other hand ,as a result of improvement in the heat exchanging between Lean and Rich solutions ,temperature of the saturated Amin solution reduces to 57°C which, consequently there is no need to use air cooler to cool running Amin. These equipments are totally omitted from the process, and its operating costs will are returned to Bidboland Gas Refinery .Finally, it was revealed that using the new heat exchanger causes a capital-return to 114864 $ annually as a result of reducing energy consumption in Reboiler and air cooler.
机译:Bidboland天然气精炼厂的问题之一,特别是在寒冷季节,是进入天然气精炼厂的酸性气体温度低,这一问题直接影响到Amin-Amin交换器的产量降低,从而导致天然气燃料消耗增加在Amin回收塔的再沸器中,因为Amin-Amin交换器无法在当前条件下根据制造商公司的设计将Rich DEA解决方案加热到最佳温度。为了解决此问题,Amin-Amin交换器通过使用Aspen Hysys专用软件进行重新设计,并通过使用Aspen Hysys软件将其用于过程中。根据获得的结果,如果使用新的交换器,则富DEA溶液的温度将从33°C升高至温度升高98°C可使再沸器的气体消耗减少33.2%。另一方面,由于改善了稀溶液和浓溶液之间的热交换,饱和Amin溶液的温度降低到57°C,因此,无需使用空气冷却器来冷却运行中的Amin。这些设备从生产过程中完全省去了,其运营成本将返还给Bidboland天然气精炼厂。最后,由于使用新的换热器,从而减少了Reboiler的能源消耗,每年的资本回报为114864 $和空气冷却器。

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