For long-running light load,the motor efficiency and power factor would be reduced,increasing the loss of motor and drag system.For the original equipment motor of the die-casting machine,one cycle of its work was most in the empty state,and the maximum impact load was only 45%.Used the high efficiency motor of the matching actual working conditions to replace the original motor.The actual power saving was about 4.7% after actual field application,and the payback period was reasonable.%对于长期运行轻载的电机,效率和功率因数都会大幅降低,导致电机和拖动设备系统损耗增加.针对压铸机原配套电机进行现场测试发现,其工作一个周期中大部分时段处于空载状态,最大冲击负载仅为45%.采用更换与之实际工况匹配的高效电机,现场应用后实际节电约4.7%,投资回收期合理.
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