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Installation of the Longest High-Performance and Rotating 11-3/4' Solid Expandable Liner on a HPHT Infill Well with Narrow Mud Weight Window

机译:安装最长的高性能并旋转11-3 / 4“固体可膨胀衬垫,在HPHT填充井上井下井下夹层

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This paper discusses installation of the longest high-performance (HP) and rotating 11-3/4" expandable liner on the Elgin field in the Central-North Sea sector of the UK that enabled isolating weak layers in the overburden formations on EIE well, providing sufficient mud weight window to permit drilling high pressure and gas bearing zones. The planning and execution of this record presented challenges beyond those encountered in standard well conditions due to narrow mud weight window (NMWW) and critical requirement of zonal isolation. EIE well was the third of the 2015-2017 infill campaign on Elgin field. The well faced major challenges in the 12-1/2" section due to the NMWW which triggered the deployment of the contingent well architecture with HP 11-3/4" expandable liner. This critical requirement of zonal isolation significantly impacted the preparation and risk assessment of expandable liner operations. A new expansion assembly design was implemented to allow rotation of the 11-3/4" size system to improve the cement job quality. Moreover, all contingency procedures were significantly modified to ensure that the objective of the specific well constraints were considered. After under-reaming while drilling 12-1/4" × 14" section down to planned depth, 860m of 11-3/4" liner was run with no open hole problems. This liner was successfully rotated at bottom prior to pumping cement and fully expanded without incident. The system was successfully pressure tested prior to drill-out of the plugs and the shoe assembly was drilled with no issues. Running of an 860m HP 11-3/4" expandable liner and rotating shoe assembly on EIE well is a record (longest HP string run before was 360m) and considered as a remarkable achievement. However, liner objectives were not fully met and cement squeeze below the shoe had to be performed. Post-job investigation highlighted issues related to dart selection and related cement over-displacement, limited contingences in case of expansion pressure loss, and the ability to pull the liner to surface in a NMWW. These issues remain to be solved for optimisation of future deployments. This paper provides information on the design and operational aspects that should be considered for expandable liner operations on complex wells with NMWW. Understanding advantages and limitations of the system will open up opportunities to improve the technology and help to reduce operational risk.
机译:本文讨论了在英国中央北海部门的埃尔金领域旋转11-3 / 4“可扩展衬里的安装,使得在eie井上的覆盖层中旋转11-3 / 4”可扩展衬垫,提供足够的泥浆重量窗口以允许钻出高压和燃气区域。由于狭窄的泥浆重量窗口(NMWW)和区域隔离的关键要求,这一记录的规划和执行呈现出在标准井条件下遇到的挑战。eie好2015-2017埃尔金领域的第三次埃格尔金领域。由于NMWW,12-1 / 2“部分面临的主要挑战,这是触发了HP 11-3 / 4”可扩展衬里的偶然井建筑的部署。区域隔离的关键要求显着影响了扩张衬里操作的制备和风险评估。实施了新的扩展组装设计,以允许旋转11-3 / 4“尺寸系统,以提高水泥就业质量。此外,所有应急程序都被显着修改,以确保考虑了特定井限制的目标。在钻孔之后钻孔12-1 / 4“×14”部分,下降到计划深度,860米11-3 / 4“衬里运行,没有开孔问题。该衬里在泵送水泥之前在底部成功旋转在没有事件的情况下完全扩张。系统在钻出塞子之前测试的压力成功,并且钻井组件没有问题。在井上运行860米HP 11-3 / 4“可扩展衬垫和旋转鞋组件记录(最长的HP字符串在360米之前运行)并被视为显着的成就。但是,衬垫目标没有完全达到鞋子下方的水泥挤压。职务后调查突出了与Dart选择和相关水泥过度位移相关的问题,在膨胀压力损失的情况下有限的差异,以及以NMWW将衬垫拉到表面的能力。这些问题仍有待解决的优化未来部署。本文提供了有关设计和操作方面的信息,这些方面应考虑在具有NMWW上的复杂井上的可扩展衬垫操作。了解系统的优势和局限将开辟改进技术的机会,并有助于降低操作风险。

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